very high oil pressure
Posted: Fri Sep 03, 2010 5:37 pm
I have an unflown Nipper with a 1834 VW. The small amount of paperwork that I have relating to the engine indicate that it was built by the owner before last from a Mexican crankcase which Barry Smith machined for the larger cylinders and supplied bearings, gaskets etc.
The engine has two oil pressure relief valves. I understand that the one nearest the propeller with a long spring prevents over pressure to the oil cooler . The rear one with a short spring is the oil pressure relief valve proper.
The engine had not run for about a year following the death of the previous owner. When we started it the oil pressure was only about 20 psi at 1500 rpm ,dropping to 5 psi when warm. Investigation revealed that there was only a spring in the rear relief valve. I ordered a new piston at a refreshingly cheap non aviation price and fitted it. The oil pressure is now about 40 psi after start , but rises within about 30 seconds to 90 psi when my courage fails me and I stop it. The new piston is not a tight fit and comes out with the spring ,so I assume that it's not stuck.
I've cleaned the crankcase hole and swapped the two pistons with no effect.
Does anyone have any suggestions ?
The engine has two oil pressure relief valves. I understand that the one nearest the propeller with a long spring prevents over pressure to the oil cooler . The rear one with a short spring is the oil pressure relief valve proper.
The engine had not run for about a year following the death of the previous owner. When we started it the oil pressure was only about 20 psi at 1500 rpm ,dropping to 5 psi when warm. Investigation revealed that there was only a spring in the rear relief valve. I ordered a new piston at a refreshingly cheap non aviation price and fitted it. The oil pressure is now about 40 psi after start , but rises within about 30 seconds to 90 psi when my courage fails me and I stop it. The new piston is not a tight fit and comes out with the spring ,so I assume that it's not stuck.
I've cleaned the crankcase hole and swapped the two pistons with no effect.
Does anyone have any suggestions ?