25 Hrs checks
Posted: Wed Nov 24, 2010 6:29 pm
Of Note:
Having just completed a 25 hr check on XD I had the misfortune to find 2 lower plugs siezed. The resultant work ended up with a top end overhall, requiring one new exhaust valve, valve damaged by helicoil breakage as bit passed out of exhaust. also two solid plug inserts were required these were fitted by Park Engineering of Malton. [This company are engine rebuild specialists]
After rebuild etc, and a full set of plugs [ouch! Barry Smith and his rel's] the flight test gave 950 fpm at gross auw - not seen that before so worth the effort.
However, I would have not needed to strip the heads if I had ensured that the plug threads were fully graphited on last fitment. Beware!
Lesson for all.
cheers
JAB
Having just completed a 25 hr check on XD I had the misfortune to find 2 lower plugs siezed. The resultant work ended up with a top end overhall, requiring one new exhaust valve, valve damaged by helicoil breakage as bit passed out of exhaust. also two solid plug inserts were required these were fitted by Park Engineering of Malton. [This company are engine rebuild specialists]
After rebuild etc, and a full set of plugs [ouch! Barry Smith and his rel's] the flight test gave 950 fpm at gross auw - not seen that before so worth the effort.
However, I would have not needed to strip the heads if I had ensured that the plug threads were fully graphited on last fitment. Beware!
Lesson for all.
cheers
JAB